A major leak in a crude oil tank: Predictable and unexpected root causes

2019
Abstract A 2000 m 3 washertank at a crude oil treatment plant suffered a structural collapse, involving total loss of integrity. A fast fractureinitiated in a sector of the shell with a severe thickness reduction due to combined internal and external corrosion. The fracture bent and propagated horizontally, at the shell-roof intersection and at the joint between second and third courses, causing the almost instant opening of a large window. Due to the large initial leakage flow, the containment enclosure wall could not hold the spilled mixture of water and crude oil. The fast leaking wave damaged the breakwatersat the top of the wall, overpassed the enclosure and pushed out a sliding gate, thus causing total liquid leakage. Fracture and computational fluid dynamics models were developed to understand the origins of the failure, as well as to reconstruct the sequence of events. Deficiencies in tank construction, maintenance adequacy, and corrosion prevention were found to be the main root causes of the failure.
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